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Photo
#1) Scraping nasty, wet, soggy, stinky old foam - 300+
pounds worth!
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Photo
#2) Deck off & stringers out |
With
the center console, wiring and fittings removed, we cut through
the deck leaving an 8" shelf to the cockpit walls, bait boxes
and transom. On pulling up the deck, it was obvious that the old
foam was completely saturated with water. I used a small hand
saw, (almost like a file), and a pry bar to cut/hack/break chunks
of the foam off, photo #1. This was a really gross and wet job!
I put the hunks of foam into industrial garbage bags, all total
I got 23 bags, and 327 POUNDS of foam out of the boat. It was
evident that this foam had been saturated for some time, since
the damp environment had also deteriorated the three wooden stringers
that ran fore and aft the full length of boat. The stringers were
made of 1/2" marine plywood and covered with a single layer
of heavy fiberglass cloth. It was obvious that the starboard stringer
was cracked, (why the trailer had indented that side), and that
the center and port ones were very rotten under the glass. I'm
very glad I chose not to use the boat much with the hull in this
condition! Picture #2 above shows the hull with the deck off,
foam out and stringers removed. Using wooden wedges, we were able
to peal up most of the fiberglass used to hold the stringers in
place. Anything left was sanded with a disk sander. Itch, itch,
itch.... You also can't spend enough on a respirator.

Photo #3) Underside of deck - one heavy sucker!
I thought it odd that Mako built the bottom with only three stringers,
but put six under the deck! The deck was very well built and weighed
a lot! It also had 1/2" x 14" plywood running side to
side for support and to bolt the console into. The PVC tube that
the teleflex and wiring ran through was very permanently fiberglassed
in, we had a devil of a time with it when lifting the deck. Eventually
we cut it out completely, as you may be able to see on the extreme
left of the picture above.
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Photo #4) Detail of stringers
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Photo #5 Dave glassing in new
stringers |
The original stringers were replaced with new ones cut to the
same size and length. Additionally, intermediate stringers were
installed, made from 4" PVC cut in half to form a "C"
section. This gave us 7 stringers in the bottom, each covered
with a minimum of 2 layers of heavy cloth and resin. Extra care
was taken to hand roll out all the air bubbles and we allowed
a week in the summer sun between layers of glass to let it really
set up. A center support, heavier than the original, was reinstalled
amidships with blocks glued by west system and fiberglassed. This
ties all three stringers together to prevent them from torqing
and provides support for the deck under the console. (A great
deal of weight is concentrated on this spot because the fuel tanks
are stored under the console, above the support) The edge of the
deck left attached to the hull, and the edge of the large section
removed, were each sanded to a sharp taper. This approx three
inches of sanding would allow us to lay new cloth and not have
a "bump" when we reattached the deck. As seen in photo
#6 below, a flange was created out of marine plywood held in place
with counter sunk stainless screws and glued with west system.
(The only purpose of the flange was to give us something to rest
the deck on so we could re-fiberglass it.)

Photo #6) Deck flange installed
Before
the deck was reattached, the PVC tube that the control cables
ran through had to be refitted. I was in a pickle because I discovered
the original was a size no longer available. With some fiberglass
and the help of another friend who found me an NOS female/female
connector, we were able to salvage the original. After several
muscle pulling test fittings, we got the deck to lay into our
flange nicely. It was west systemed to the flange and screwed
in place. Two to three new layers of fiberglass were laid over
the cut. Again, all the air bubbles had to be rolled out of the
cloth, and we had to allow the resin several days to set up between
layers. The new fiberglass and the old non-skid that was molded
into the gel-coat on the deck all had to be sanded down to be
nice and smooth and flush. This took a lot of time and sweat.
By now I had developed a resistance to the fiberglass itchies!
My ventilator and belt sander were earning their keep! As seen
in photo #7, we had to be patient and sand and mud with a marine
filler, (like bondo), to get everything nice and smooth.

Photo #7) Deck on again!
I gave the deck two coats of a marine epoxy primer. (This took
it's sweet time to cure since the cool fall days had set in!)
The last step was to give it a nice coat of epoxy gray paint and
shake some non-skid into it, photo #8. (The new non-skid works
much better than the original that was molded into the gel) As
you can see, I taped off the white waterways and around the edge.
This gave it a nice clean original look, and makes it so the difference
in non-skid from the deck to the forward platform is hardly noticeable.
I also mixed up some of the new closed cell 2 part foam and filled
most of the space between the hull and deck. Hopefully it will
react better over time than the original!

Photo # 8) Deck done at last!
The boat floats right on it's original marks, (about 3 1/2"
higher than before!!!) it rides and handles better than it has
in decades. A great fringe benefit is a 30% increase in fuel economy
from my '90 Johnson 115 because the boat is stiff and planes much
more easily. She also will make 38 knots at WOT, about 5 knots
better than it did before. I also sleep better knowing the hull
is sound and the flotation will errrrr.... float! I am very proud
of my old boat, and think that she was well worth all the work.
I owe a great debt of thanks to Dave & Sheila for taking this
project on - without their expertise and masterful work, there
is no way this boat would have gone back together.
And
the Engine!
1990
Johnson 115hp |

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Year & Model: 1990 Johnson
Horsepower: 115@5,500 rpm
Cylinders: 90 degree
V-4
Bore: 3.500"
Stroke: 2.588"
Ignition: CD
Point Gap: none
Cooling: Water by rubber impeller
Condition: Unrestored
Retail price when new: $NA
Weight: 325 lbs.
Oil/Gas Mix: 50:1 (VRO removed & tossed!)
Spark Plug: NGK BR9HS
Comments:
My newest outboard ever! Quiet, reliable and fairly easy
to work on (except the $#@*&! thermostats) Fuel economy
on the old Mako is excellent burning about 3-4 gallons an
hour at 2500-3500 rpms. At full throttle fuel consumption
is 6 gph. |
Epilogue
I
wrote Mako Marine about my boat and received an interesting reply
- they had never heard of a boat as old or with as low a hull
number as mine! Apparently the oldest Mako they were aware of
was from 1968. I also did some research via the DMV and contacted
the original owner and second owner of the boat. I learned that
the boat was delivered to the Darien Bait Shop in March or April
of 1967. Each of the owners sent me pictures and stories of the
boat during their ownership and the second owner even stopped
by and visited with me!
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Here is my Mako
in the 1970's courtesy of the boat's second owner. (nice
electric shift Evinrude!) |
And the Mako today. |